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Occupational Safety and Health Administration OSHA

Inspection Detail

Case Status: CLOSED
Inspection: 530858.015 - Elkhorn Construction Inc.

Inspection Information - Office: Englewood

Nr: 530858.015Report ID: 0830600Open Date: 06/25/2012

Elkhorn Construction Inc.
35191 Hwy 160
Bayfield, CO 81122
Union Status: NonUnion
SIC:
NAICS: 211111/Crude Petroleum and Natural Gas Extraction
Mailing: P.O. Box 809, Evanston, WY 82930

Inspection Type:Unprog Rel
Scope:Complete Advanced Notice:N
Ownership:Private
Safety/Health:Safety Close Conference:08/01/2012
Emphasis: L:OilgasClose Case:08/26/2013

Related Activity:TypeIDSafetyHealth
 Accident407450    
Case Status: CLOSED

Violation Summary
Serious Willful Repeat Other Unclass Total
Initial Violations 1 1
Current Violations
Initial Penalty $7,000 $0 $0 $0 $0 $7,000
Current Penalty $0 $0 $0 $0 $0 $0
FTA Amount $0 $0 $0 $0 $0 $0

Violation Items
# ID Type Standard Issuance Abate Curr$ Init$ Fta$ Contest LastEvent
Deleted 1. 01001 Serious 5A0001 12/19/2012 02/07/2013 $0 $7,000 $0 01/09/2013 F - Formal Settlement

Accident Investigation Summary
Summary Nr: 33816.015Event: 06/25/2012One Employee Is Killed And Two Employees Are Injured When A
At approximately 8:00 a.m. on June 25, 2012, an employee was at the side of the pig launcher. The process was to purge the line of carbon gas with nitrogen. The nitrogen was pumped by a rig used to frac wells. The pump truck was capable of creating pressures which were several times greater than the launcher was designed and built for. The employee had several responsibilities some of which were to check the joints of black pipe feeding the nitrogen. This entailed pouring soap water on the joints and check for bubbles. He was also responsible for watching the pressure gauges on the launcher, getting the line purged so the pigging operation could start, and opening and closing the ball valves in the line to provide for proper flow. He had just spoken to another employee while looking at the gauges on the launcher when the launcher ruptured. The ball valve leading to the 16-in. main line was not open. The pump truck had been pushing nitrogen into the small pig launcher instead of over three mile long pipeline. The gauges were not reading any pressure at all and when the pump truck kicked up the pressure, the launcher ruptured. The launcher was shot over 800 feet away. The main part of the vessel struck another employee killing him instantly. During the ILI inspection of gas pipeline a pig is used to clean, examine, and test the pipeline. The crew was using a Halliburton pumper truck used for fracing operations. The pumper was sending nitrogen down the line to purge the carbons. An error in valve positioning occurred when the ball valve was left closed to the main line. The pumper truck far exceeded the specs that the pig launcher was built to. The launcher ruptured and killed one while injuring two more employees.
Keywords: pipe, struck by, explosion, nitrogen, flying object, compressed gas
Inspection Degree Nature Occupation
1 530858.015 Fatality Cut/Laceration

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