Inspection Detail
Inspection: 303825855 - Cott Beverages Usa Inc
Inspection Information - Office: Nc Department Of Labor - Raleigh
Site Address:
Cott Beverages Usa Inc
4843 International Blvd
Wilson, NC 27893
Mailing Address:
4843 Novopharm Blvd. W, Wilson, NC 27893
Union Status: NonUnion
SIC:3085
NAICS: 0
Inspection Type: Complaint
Scope: Partial
Advanced Notice: N
Ownership: Private
Safety/Health: Health
Close Conference: 08/17/2000
Emphasis: S:Program Improvements
Case Closed: 11/15/2000
| Type | Activity Nr | Safety | Health |
|---|---|---|---|
| Accident | 100352822 | ||
| Complaint | 202891511 | Yes |
| Violations/Penalties | Serious | Willful | Repeat | Other | Unclass | Total |
|---|---|---|---|---|---|---|
| Initial Violations | 2 | 1 | 3 | |||
| Current Violations | 2 | 1 | 3 | |||
| Initial Penalty | $1,788 | $0 | $0 | $0 | $0 | $1,788 |
| Current Penalty | $1,252 | $0 | $0 | $0 | $0 | $1,252 |
| FTA Penalty | $0 | $0 | $0 | $0 | $0 | $0 |
| # | Citation ID | Citaton Type | Standard Cited | Issuance Date | Abatement Due Date | Current Penalty | Initial Penalty | FTA Penalty | Contest | Latest Event | Note |
|---|---|---|---|---|---|---|---|---|---|---|---|
| 1. | 01001A | Serious | 19100120 Q06 III | 09/12/2000 | 10/15/2000 | $963 | $1,375 | $0 | I - Informal Settlement | ||
| 2. | 01001B | Serious | 19100120 Q02 II | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 3. | 01001C | Serious | 19100120 Q03 III | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 4. | 01001D | Serious | 19100120 Q03 IV | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 5. | 01001E | Serious | 19100120 Q06 I | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 6. | 01001F | Serious | 19100120 Q06 V | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 7. | 01001G | Serious | 19100134 C01 | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 8. | 01001H | Serious | 19100134 C03 | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 9. | 01001I | Serious | 19100134 E01 | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 10. | 01001J | Serious | 19100134 F01 | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 11. | 01001K | Serious | 19100134 H02 I | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 12. | 01001L | Serious | 19100134 H03 IVA | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 13. | 01001M | Serious | 19100134 K01 | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 14. | 01001N | Serious | 19101200 H01 | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 15. | 01002 | Serious | 19101450 F02 | 09/12/2000 | 10/15/2000 | $289 | $413 | $0 | I - Informal Settlement | ||
| 16. | 02001A | Other | 19100157 C01 | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - | ||
| 17. | 02001B | Other | 19100157 G01 | 09/12/2000 | 10/15/2000 | $0 | $0 | $0 | - |
Investigation Summary
At approximately 9:30 p.m. on or about July 31, Employee #1, a maintenance technician for a can and bottling operation, responded to a possible ammonia leak during the second shift at the plant. A 2,000 lb outside storage tank pumped ammonia into the line-filled room to cool the syrups to between 35 and 40 degrees F before the cans and bottles were filled. Apparently, part of the Hanson valve, which controlled the line flow, broke and ammonia had leaked into the air. Employee #1 arrived and entered the maintenance room without any respiratory PPE. Once the supervisor was present, however, all the maintenance technicians donned respirators and were able to isolate the line where the leak occurred. The plant was evacuated and the lead maintenance technician and the second shift supervisor toured the facility with ammonia strips to determine whether it was safe to re-enter. Ammonia was detected throughout the plant, so the second shift employees were sent home and all the doors were opened to allow the buildings to air out. Employee #1 said he felt nauseous and had a headache, and the supervisor sent him to the Emergency Room. After determining the plant was safe to enter, the supervisor and maintenance lead decided to allow the third shift to begin work. Shortly thereafter, several employees in different parts of the building began to experience burning sensations on their faces and in their noses and respiratory tract. Even after stepping outside, these employees did not feel better, so the supervisor sent them to the hospital as a precaution. The supervisor and maintenance lead then called the plant manager and requested permission to send the third shift home. Employee #1 and coworkers were treated and released, although Employee #1 was instructed by the doctor to take one day off from work. The location of the ammonia leak was in the compressor room, not the filler room, where there was a control panel that would shut down the system if a drop in pressure was detected, as happened in this case. Preventive maintenance was performed on the regulator valves, but not on the gaskets. In this case, the failure occurred due to a pinhole in a gasket. According to the lead maintenance technician, there was no way to prevent the occurrence. Because the refrigeration system was a closed loop, the tank had never been refilled in the 3 years the plant has been in operation. It was later determined that between 50 and 75 lb of hot vapor had been released.
Keywords: LEAK, VAPOR, GASKET, AMMONIA, INHALATION, AIR CONTAMINATION, RESPIRATORY TRACT, CHEMICAL VAPOR, ACCIDENTAL DISCHARGE
| # | Inspection | Age | Sex | Degree of Injury | Nature of Injury | Occupation |
|---|---|---|---|---|---|---|
| 1 | 303825855 | Occupation Not Listed |
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