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Inspection Detail

Inspection: 1811157 - Lockheed California Company

Inspection Information - Office: Region 09; San Francisco

 

Inspection Nr: 1811157
Report ID: 0931800
Date Opened: 04/13/1984

Site Address:
Lockheed California Company
2555 Hollywood Way
Burbank, CA 91520

Mailing Address:
, , 00000

Union Status: Union

SIC:3720

NAICS: 0 


Inspection Type: Referral

Scope: Partial

Advanced Notice: N

Ownership: Private

Safety/Health: Safety

Close Conference: 05/11/1984

Planning Guide: Safety-Construction

Emphasis:

Case Closed: 12/31/1988


Related Activity
Type Activity Nr Safety Health
Referral 900548330 Yes
Violation Summary
Violations/Penalties Serious Willful Repeat Other Unclass Total
Initial Violations 1 1 2
Current Violations 1 1 2
Initial Penalty $640 $0 $0 $0 $0 $640
Current Penalty $640 $0 $0 $0 $0 $640
FTA Penalty $0 $0 $0 $0 $0 $0

Violation Items
# Citation ID Citaton Type Standard Cited Issuance Date Abatement Due Date Current Penalty Initial Penalty FTA Penalty Contest Latest Event Note
1. 01001 Other 19100157 E03 04/20/1984 05/18/1984 $0 $0 $0 -  
2. 02001 Serious 5A0001 05/25/1984 04/13/1984 $640 $640 $0 -  

Investigation Summary

Investigation Nr: 14555072
Event: 04/13/1984
JET FUEL TANKS IN TESTING DEVICE EXPLODED

THE THREE EMPLOYEES WERE PREPARING A UNIT TESTING DEVICE CONSISTING OF FUEL COMPARTMENTS WITH INTERNAL FUEL PIPING AND SWITCHING DEVICES. THE COMPARTMENTS CONTAINED RESIDUAL JP-4 JET FUEL, WITH AN LEL OF .8% BY VOLUME AND A FLASH POINT OF -4% F. WRITTEN SOP INSTRUCTIONS PRESCRIBED CLEANING AND VENTING TO REDUCE THE VAPORS TO LESS THAN 10% OF THE LEL. GAS FREEING WAS TO BE DONE AFTER ALL ELECTRICAL POWER AND ALL OTHER SOURCES OF IGNITION WERE REMOVED FROM THE UNIT AND SURROUNDING AREA. NO SYNTHETIC CLOTHING MATERIALS WAS TO BE ALLOWED IN THE WORK AREA. ALSO, CHECK LISTS WERE TO BE COMPLETED FOR ALL THE ABOVE, PLUS TESTING WAS TO BE ACCOMPLISHED WITH A COMBUSTIBLE GAS INDICATOR. WORK WAS PERMITTED TO PROCEED WITHOUT GAS FREEING AND TESTING, AND WITHOUT A POSITIVE DETERMINATION THAT ALL ELECTRICAL CIRCUITS WERE DEENERGIZED AND THAT WORKERS WERE NOT WEARING SYNTHETIC TYPE CLOTHING. THE RELATIVE HUMIDITY WAS 23% AT 80 DEGREES FARENHEIT. A SPARK, MOST LIKELY FROM AN ELECTRICAL CIRCUIT (28 VOLTS) TO A PRESSURE SWITCH, PROBABLY IGNITED THE VAPORS. CAUSE OF ACCIDENT: SOP WAS NOT FOLLOWED OR ENFORCED.

Keywords: ELECTRIC ARC, FLAMMABLE VAPORS, VENTING, CLEANING, EXPLOSION, JET FUEL, TANK

Investigated Inspection
# Inspection Age Sex Degree of Injury Nature of Injury Occupation
1 1811157 Hospitalized injury Burn/Scald(Heat) Occupation not reported
2 1811157 Hospitalized injury Burn/Scald(Heat) Occupation not reported
3 1811157 Hospitalized injury Burn/Scald(Heat) Occupation not reported
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