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Inspection Detail

Inspection: 123650574 - Marathon Oil Company

Inspection Information - Office: Houston South Area Office

 

Inspection Nr: 123650574
Report ID: 0626700
Date Opened: 07/17/1994

Site Address:
Marathon Oil Company
10th St
Texas City, TX 77591

Mailing Address:
P.O.Box 1191, Texas City, TX 77592

Union Status: Union

SIC:2911

NAICS: 0 


Inspection Type: Accident

Scope: Partial

Advanced Notice: N

Ownership: Private

Safety/Health: Health

Close Conference: 10/17/1994

Emphasis:

Case Closed: 06/09/1995


Related Activity
Type Activity Nr Safety Health
Accident 361140908
Violation Summary
Violations/Penalties Serious Willful Repeat Other Unclass Total
Initial Violations 6 6
Current Violations 2 1 3
Initial Penalty $27,200 $0 $0 $0 $0 $27,200
Current Penalty $10,200 $0 $0 $850 $0 $11,050
FTA Penalty $0 $0 $0 $0 $0 $0

Violation Items
# Citation ID Citaton Type Standard Cited Issuance Date Abatement Due Date Current Penalty Initial Penalty FTA Penalty Contest Latest Event Note
1. 01001 Other 19100119 C02 11/07/1994 03/12/1995 $850 $4,250 $0 I - Informal Settlement  
2. 01002A Serious 19100119 D03 IB 11/07/1994 12/12/1994 $4,250 $4,250 $0 I - Informal Settlement Citation has been deleted.
3. 01002B Serious 19100119 J06 II 11/07/1994 12/12/1994 $0 $0 $0 I - Informal Settlement Citation has been deleted.
4. 01003 Serious 19100119 F01 IB 11/07/1994 12/12/1994 $4,250 $4,250 $0 I - Informal Settlement Citation has been deleted.
5. 01004 Serious 19100119 F01 IIIB 11/07/1994 02/12/1995 $4,250 $4,250 $0 I - Informal Settlement  
6. 01005 Serious 19100119 F04 11/07/1994 12/12/1994 $4,250 $4,250 $0 I - Informal Settlement Citation has been deleted.
7. 01006 Serious 19100119 J04 II 11/07/1994 04/12/1995 $5,950 $5,950 $0 I - Informal Settlement  

Investigation Summary

Investigation Nr: 14406912
Event: 07/15/1994
Employee killed when exposed to caustic acid-soluble oil

At approximately 8:00 p.m. on July 16, 1994, Employee #1, an operator in the alky unit of an oil refinery, was between the acid regeneration system and the neutralization system. The level in the rerun tower (part of the acid regeneration system) was controlled by an automatic level control valve (92LC0102), which allowed the stream to flow to the ASO neutralization system. A line break at a T just past this control valve occurred while Employee #1 was trying to remove a bull plug from a 3/4 in. bleeder pipe. Employee #1 told the stillman that he was trying to correct a blockage in the line. The method he was using was not a normal method commonly used by the operators interviewed, and according to the alky unit operators, the operation that Employee #1 was performing did not have written operating procedures. The bleeder pipe that broke from the T was approximately 17 in. long with the Durco valve about 4 in. from the break and about 10 in. from the break to another T containing a bull plug. Another bull plug was also on the end of the bleeder. The P and IDs did not show this configuration for this bleeder. Employee #1 was exposed to acid-soluble oil or ASO, which contains 5 to 20 percent HF. He suffered chemical burns and was killed.

Keywords: PIPE PLUG, CAUSTIC, WORK RULES, EQUIPMENT FAILURE, CHEMICAL BURN, PIPE, REFINERY

Investigated Inspection
# Inspection Age Sex Degree of Injury Nature of Injury Occupation
1 123650574 Fatality Burn(Chemical) Miscellaneous plant and system operators
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