Powered by GoogleTranslate

Inspection Detail

Inspection: 311006605 - Boomer Well Service

Inspection Information - Office: Oklahoma City Area Office

 

Inspection Nr: 311006605
Report ID: 0627700
Date Opened: 05/29/2008

Site Address:
Boomer Well Service
White 3-1
Woodward, OK 73802

Mailing Address:
P.O. Box 608, Woodward, OK 73802

Union Status: NonUnion

SIC:1389

NAICS: 213112/Support Activities for Oil and Gas Operations


Inspection Type: Accident

Scope: Partial

Advanced Notice: Y

Ownership: Private

Safety/Health: Safety

Close Conference: 10/21/2008

Planning Guide: Safety-Manufacturing

Emphasis: L:Oilgas

Case Closed: 01/04/2010


Related Activity
Type Activity Nr Safety Health
Accident 100645811
Violation Summary
Violations/Penalties Serious Willful Repeat Other Unclass Total
Initial Violations 3 3
Current Violations 3 3
Initial Penalty $6,250 $0 $0 $0 $0 $6,250
Current Penalty $3,750 $0 $0 $0 $0 $3,750
FTA Penalty $0 $0 $0 $0 $0 $0

Violation Items
# Citation ID Citaton Type Standard Cited Issuance Date Abatement Due Date Current Penalty Initial Penalty FTA Penalty Contest Latest Event Note
1. 01001 Serious 19100023 C01 11/12/2008 12/01/2008 $1,500 $2,500 $0 I - Informal Settlement  
2. 01002 Serious 5A0001 11/12/2008 11/25/2008 $750 $1,250 $0 I - Informal Settlement  
3. 01003 Serious 5A0001 11/12/2008 12/15/2008 $1,500 $2,500 $0 I - Informal Settlement  

Investigation Summary

Investigation Nr: 200644110
Event: 05/28/2008
Employee Is Killed When Struck by Pressurized Hose

On May 28, 2008, employees were opening an existing well to put it back on line to produce gas. The well-servicing employees and the trucking/servicing company, contracted to pump fluid down the casing to kill the well, had come off break. According to both companies, the well was dead, with a pressure between 0 psi to10 psi reported by the pump operator. The pump operator was maintaining a velocity of 0.25 barrels (bbl) of fluid per minute into the well, when the servicing employees noticed the well gassing out the tubing. The servicing employees went to shut in the well and move the pump hose from the casing valve to the TIW (Texas Iron Works) valve. The pump continued to operate at 0.25 bbl per minute when the casing valve was shut. As the employees started to remove the hose, the back pressure blew the hose off the fitting and struck Employee #1. Employee #1 was killed.

Keywords: GAS WELL, WELL, GAS, HOSE, HIGH PRESSURE, GAS LEAK, STRUCK BY

Investigated Inspection
# Inspection Age Sex Degree of Injury Nature of Injury Occupation
1 311006605 Fatality Bruise/Contus/Abras Occupation not reported
Back to Top

Thank You for Visiting Our Website

You are exiting the Department of Labor's Web server.

The Department of Labor does not endorse, takes no responsibility for, and exercises no control over the linked organization or its views, or contents, nor does it vouch for the accuracy or accessibility of the information contained on the destination server. The Department of Labor also cannot authorize the use of copyrighted materials contained in linked Web sites. Users must request such authorization from the sponsor of the linked Web site. Thank you for visiting our site. Please click the button below to continue.

Close