| <<< Back to Armour Swift-Eckrich PSM Presentation |
Printing Instructions |
U.S. Department of Labor
Occupational Safety and Health Administration
Suite 105
8600 Farley
Overland Park, KS 66212
Phone: (913)236-3220 FAX: (913)236-3224 |
 |
|
Citation and Notification of Penalty
|
To:
Armour Swift - Eckrich, Inc.
and its successors
4612 Speaker Rd.
Kansas City, KS 66110
|
Inspection Number:
301340220
Inspection Date(s): 04/09/97 - 09/26/97
Issuance Date: 10/09/97 |
Inspection
Site:
4612 Speaker Rd.
Kansas City, KS 66110 |
The violation(s) described in this
Citation and Notification of Penalty is (are) alleged to have occurred on or about the
day(s) the inspection was made unless otherwise indicated within the description given
below. |
This Citation and Notification of Penalty (this Citation) describes violations of the Occupational Safety
and Health Act of 1970. The penalty(ies) listed herein is (are) based on these violations.
You must abate the violations referred to in this Citation by the dates listed and pay the
penalties proposed, unless within 15 working days (excluding weekends and Federal
holidays) from your receipt of this Citation and Notification of Penalty you mail a notice
of contest to the U.S. Department of Labor District Office at the address shown above.
Please refer to the enclosed booklet (OSHA 3000) which outlines your rights and
responsibilities and which should be read in conjunction with this form. Issuance of this
Citation does not constitute a finding that a violation of the Act has occurred unless
there is a failure to contest as provided for in the Act or, if contested, unless this
Citation is affirmed by the Review Commission or a court.
Posting - The law requires that a copy of this Citation and
Notification of Penalty be posted immediately in a prominent place at or near the location
of the violation(s) cited herein, or , if it is not practicable because of the nature of
the employer's operations, where it will be readily observable by all affected employees.
This Citation must remain posted until the violation(s) cited herein has (have) been
abated, or for 3 working days (excluding weekends and Federal holidays), whichever is
longer. The penalty dollar amounts need not be posted and may be marked out or covered
up prior to posting.
Informal Conference - An informal conference is not required.
However, if you wish to have such a conference you may request one with the District
Director during the 15 working day contest period. During such an informal conference you
may present any evidence or views which you believe would support an adjustment to the
citation(s) and/or penalty(ies),
If you are considering a request for an informal conference to discuss
any issues related to this Citation and Notification of Penalty, you must take care to
schedule it early enough to allow time to contest after the informal conference, should
you decide to do so. Please keep in mind that a written letter of intent to contest must
be submitted to the District Director within 15 working days of your receipt of this
Citation. The running of this contest period is not interrupted by an informal conference.
If you decide to request an informal conference, please complete,
remove and post the page 3 Notice to Employees next to this
Citation and Notification of Penalty as soon as the time, date, and place of the informal
conference have been determined. Be sure to bring to the conference any and all supporting
documentation of existing conditions as well as any abatement steps taken thus far. If
conditions warrant, we can enter into an informal settlement agreement which amicably
resolves this matter without litigation or contest.
Right to Contest - You have the right to contest this Citation
and Notification of Penalty. You may contest all citation items or only individual items.
You may also contest proposed penalties and/or abatement dates without contesting the
underlying violations. Unless you inform the District Director in writing that
you intend to contest the citation(s) and/or proposed penalty(ies) within 15 working days
after receipt, the citation(s) and the proposed penalty(ies) will become a final order of
the Occupational Safety and Health Review Commission and may not be reviewed by any court
or agency.
Penalty Payment - Penalties are due
within 15 working days of receipt of this notification unless contested. (See the enclosed
booklet and the additional information provided related to the Debt Collection Act of
1982.) Make your check or money order payable to "DOL-OSHA". Please indicate the
Inspection Number on the remittance.
OSHA does not agree to any restrictions or conditions or endorsements
put on any check or money order for less than the full amount due, and will cash the check
or money order as if these restrictions, conditions, or endorsements do not exist.
Notification of Corrective Action - For violations which you do
not contest, you should notify the U.S. Department of Labor District Office promptly by
letter that you have taken appropriate corrective action within the time frame set forth
on this Citation. Please inform the District Office in writing of the abatement steps you
have taken and of their dates, together with adequate supporting documentation, e.g.,
drawings or photographs of corrected conditions, purchase/work orders related to abatement
actions, air sampling results, etc.
Employer Discrimination Unlawful - The law prohibits
discrimination by an employer against an employee for filing a complaint or for exercising
any rights under this Act. An employee who believes that he/she has been discriminated
against may file a complaint no later than 30 days after the discrimination occurred with
the U.S. Department of Labor District Office at the address shown above.
Employer Rights and Responsibilities - The enclosed booklet
(OSHA 3000) outlines additional employer rights and responsibilities and should be read in
conjunction with this notification.
Notice to Employees - The law gives an employee or his/her
representative the opportunity to object to any abatement date set for a violation if
he/she believes the date to be unreasonable. The contest must be mailed to the U.S.
Department of Labor District Office at the address shown above and postmarked within 15
working days (excluding weekends and Federal holidays) of the receipt by the employer of
this Citation and Notification of Penalty.
Citation 1 Item 1 Type of Violation: Serious
Section 5(a)(1) of the Occupational Safety and Health Act of
1970: The employer did not furnish employment and a place of employment which were free
from recognized hazards that were causing or likely to cause death or serious physical
harm to employees in that employees were exposed to falling blast doors:
- At the establishment employee(s) moving carts of product into
or out of the freezers or ovens were exposed to physical injuries caused by blast doors
falling on employee(s). Employee(s) were raising the blast doors using the chain hoist
mechanism, then latching the chain to a pvc clamp screw where the chain would slip off
allowing the blast doors to fall.
- Blast doors raised by employee(s) without the
chain mechanisms were exposing employee(s) to physical injuries created by placing a pole
under the blast doors. The pole would be inadvertently hit by the cart causing the blast
doors to fall hitting the employee(s).
Among other methods, one feasible and acceptable abatement method
to correct this hazard is to conduct periodic inspections of the blast doors and correct
deficiencies when noted.
| Date By Which Violation Must be Abated: |
11/08/97 |
| Proposed Penalty: |
$3150.00 |
Citation 1 Item 2 Type of Violation: Serious
29 CFR 1910.38(a)(5)(ii)(C): The employer
did not review the Emergency Action Plan with each employee covered by the plan whenever
the plan was changed:
- At the facility, the Emergency Action Plan
had undergone revisions between April 16, 1992 and March 14, 1997, which changed the
method of notification for a hazardous chemical leak from using the fire alarm, to using
an announcement over the intercom by the most senior official on duty, without employee(s)
being trained on the change in alarm procedures.
- At the facility, the Emergency Action Plan
had undergone revision on February 15, 1997 which changed the means of egress route near
the cafeteria area, without changes being immediately made to the escape route maps and
without training employee(s) in the change in the means of egress routes.
| Date By Which Violation Must be Abated: |
12/08/97 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 3 Type of Violation: Serious
29 CFR 1910.119(c)(1): The employer did not develop a written plan of
action regarding the implementation of the employee participation required by 29 CFR
1910.119:
- At the facility , the Employee Participation Guidelines did
not address how employee(s) and their representatives would be consulted in the
development of the following elements of process safety management:
- Employee Participation
- Contractor Programs and Evaluations
- Hot Work
- Management of Change
- At the facility, the Employee Participation Guidelines did
not assign responsibility and authority for implementing the various elements of the PSM
standard nor did it explain how plant personnel would interface with corporate personnel
designing and specifying new systems.
| Date By Which Violation Must be Abated: |
01/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 4 Type of Violation: Serious
29 CFR 1910.119(c)(2): The employer did not consult with employees and
their representative on the conduct and development of process hazard analyses and on the
development of the other elements of process safety management:
- The employer did not consult with employee(s) and their
representatives on the following elements of process safety management:
- How to obtain and verify the process safety information pertaining
to the hazardous chemicals, technology, and equipment in the process.
- The methodology appropriate to determine and evaluate hazards of the
process including facility siting and human factors.
- The establishment of a system to promptly address the teams findings
and recommendations and to communicate the actions to operating, maintenance, and other
employee(s) whose work assignments are in the process.
- Who should assist in developing operating procedures, which
operating procedures should be developed, what format should be used, and how to certify
annually that the operating procedures were current and accurate.
- What training was required for operators before they could operate
the process alone. What the content and frequency of refresher training should be. How
could the employer ascertain operators received and understood the training.
- How contractor safety performance and programs should be evaluated
both prior to selection and periodically while on site. How work practices to control
entrance, presence, and exit or contract employers and contract employee(s) should be
developed and implemented.
- How should a pre-startup safety review be performed, who should
perform it.
- Which equipment should be included in the mechanical integrity
program. What written procedures are needed to maintain the on-going integrity of process
equipment and test and inspection equipment. What training employee involved in
maintaining the equipment should have, and what special certifications are necessary. What
procedures including reporting and assignment of responsibility are necessary to assure
deficiencies are corrected in a timely manner. What procedures are necessary to assure
equipment is fabricated and installed consistent with design specifications and that spare
parts are suitable for the process.
- How should the hot work permit be implemented.
- What is a change, and how should management of change be
implemented.
- Which incidents and near misses should be reported and
investigated. Who should be on the team, what technique should be used to thoroughly
investigate and analyze the incident. What system should be implemented to promptly
resolve report findings and recommendations. How should results be reviewed with
employee(s).
- Who should be involved with the compliance audit, how should
findings be addressed and deficiencies corrected.
- Neither the Contractor Safety Program nor the Employee
Participation Guidelines, established a method to inform all contractor employee(s) and their representatives that their process safety
concerns and suggestions are welcome, and did not solicit the advice and suggestion of contractor employee(s) working
in the process about specific aspects of process safety.
| Date By Which Violation Must be Abated: |
01/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 5 Type of Violation: Serious
29 CFR 1910.119(d)(2)(i): The employer did not develop a written
compilation of process safety information pertaining to the technology of the process,
which included those elements specified in 29 CFR 1910.119(d)(2)(i)(A),(C),(D)and(E):
- At the facility, the compilation of process safety information for
the old ammonia refrigeration units did not include information pertaining to the
technology of the process including a block flow diagram or simplified process flow
diagram.
- At the facility, the compilation of process safety information for
the old and new ammonia refrigeration units did not include information pertaining to the
technology of the process including the maximum inventory of vessels including the 75
pound accumulator, the 35 accumulator, and ammonia surge drums and receivers.
- At the facility, the compilation of process safety information for
the old and new ammonia refrigeration units did not include information pertaining to the
technology of the process including safe upper and lower limits for such items as
temperatures, pressure, flow, or levels.
- At the facility, the compilation of process safety information for
the old and new ammonia refrigeration units did not include information pertaining to the
technology of the process including deviation from safe upper and lower limits such items
as temperatures, pressure, flow, or levels.
| Date By Which Violation Must be Abated: |
02/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 6 Type of Violation:
Serious
29 CFR 1910.119(d)(3): The employer did not develop a written
compilation of process safety information pertaining to the equipment in the process,
which included those elements specified in 29 CFR 1910.119(d)(3)(i)(A),(B),(C),(D),(E) and
(H):
- At the facility, the compilation of process safety information for
the old and new ammonia refrigeration units did not include information which included
design codes and standards used; materials of construction, anticipated corrosion rates,
specified minimum wall thickness for equipment such as pressure vessels and piping
including, but not limited to, the hot gas return lines, high temperature liquid lines,
hot gas lines, relief valve headers, and pressure relief valves. For the new ammonia
refrigeration unit the compilation of process safety information did not include materials
of construction for equipment such as but not limited to compressor, compressor oil pumps,
surge drums, ammonia pumps, and pressure relief valves.
- At the facility, the compilation of process safety information for
the old and new ammonia refrigeration units did not include information which included
piping and instrument diagrams (PI&Ds).
- At the facility, the compilation of process safety information for
the old and new ammonia refrigeration units did not include information concerning
electrical classifications of machine rooms.
- At the facility, the compilation of process safety information for
the old and new ammonia refrigeration units did not include information on relief system
design and design basis.
- At the facility, the compilation of process safety information for
the old and new ammonia refrigeration units did not include information on ventilation
system design and it relationship to the classification of electrical wiring.
- At the facility, the compilation of process safety information for
the old and new ammonia refrigeration units did not include information on safety
systems (e.g. interlocks, cutouts, detection and suppression systems).
| Date By Which Violation Must be Abated: |
02/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 7 Type of Violation:
Serious
29 CFR 1910.119(d)(3)(ii): The employer did not document that the equipment in the process
complied with recognized and generally accepted good engineering practices:
- At the facility, the employer did not "walk the line" to determine that the
equipment in the refrigeration systems met good engineering design including:
- the location for the discharge of pressure relief valves for the new system
- the size of the common vent header that pressure relief valves are manifolded into
- pipe and vessels insulation materials and coatings were suitable for the application
- The 25# and 3# accumulators were not equipped with pressure relief devices
- In the old unit, king valves which stop the flow of liquid ammonia were not operable
from the floor nor was a fixed platform for access provided.
- At the facility, the employer did not verify that the old and new machine room
complied with recognized and generally accepted good engineering practices in that the
need for Class 1, Division 2 electrical classification was not addressed, nor was the need
to provide and locate emergency remote controls, to stop the action of the refrigeration
compressors and to activate the emergency ventilation system, immediately outside the
machinery room addressed.
| Date By Which Violation Must be Abated: |
01/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 8 Type of Violation: Serious
29 CFR 1910.119(e)(1): The employer did not perform an initial process analysis
appropriate to the complexity of the process to identify, evaluate, and control hazards
involved in the process:
- The process hazard analysis conducted on the old system in 1994 was not of appropriate
complexity to identify the following hazards:
- Over tightening of the valve causing bonnet to lift
- The effect of water hammer or slugging in an ammonia pipe/valve
- Leaving hand-valve open or close without periodic cycling
- An automatic valve opening/closing with excessive force
- Ammonia leak from corrosion or ammonia piping in an enclosed area
- Isolation of line full of ammonia
- Gasket or flanges failures
- Inadequate preventive maintenance on instrumentation/controls
- Critical instrumentation being taken out of service
- SRV capacity is too low or venting to an unsafe area
- Stress corrosion cracking in vessels including accumulators and receivers
- The process hazard analysis conducted on the old system in 1994 was not of
appropriate complexity to evaluate and control the following hazards:
- Ammonia leak from accumulator, piping, or level indicator in an enclosed area or on
roof.
- Failure of solenoid valve to cycle from low side dumps with resulting vibration and
possible leaking from hydraulic hammer in liquid line to the receiver.
- Ammonia leak from stems on valves in an enclosed area.
- Ammonia leak from corrosion of ammonia piping in an enclosed area.
- Isolation of line full of ammonia.
| Date By Which Violation Must be Abated: |
03/01/98 |
| Proposed Penalty: |
$7000.00 |
Citation 1 Item 9a Type of Violation: Serious
29 CFR 1910.119(e)(3)(ii): The process hazard analysis did not address previous incident
which had a likely potential for catastrophic consequences in the workplace:
The process hazard analysis for the old system did not include an evaluation of the
following incidences which occurred prior to the completion of the process hazard analysis
such as, but not limited to:
| 1-25-92 |
Lost low side because liquid level alarm
didn't work |
| 1-25-92 |
#1 dump valve doesn't reseat all the times |
| 2-03-92 |
Need 3000A valve for #1 dump high side,
hang ups |
| 2-09-92 |
Repaired ammonia leaks row #5, liquid line |
| 2-23-92 |
Repaired hot gas coil in manufacturing for
row #6 |
| 3-10-92 |
Transfer tank went on the fritzs |
| 3-18-92 |
Valve seems to be stuck for hot gas
solenoid for row #6 |
| 3-31-92 |
Lost engine room for no apparent reason |
| 4-05-92 |
#2 temp cooler suction valve is hung |
| 4-05-92 |
Bad low temperature probe in oil separator
for #7 FES compressor |
| 4-11-92 |
TRM cooler #2 using 30 amp fuse instead of
15 amp fuse |
| 4-13-92 |
Hi temp liquid line valve is stuck, burning
up coils very quickly |
| 4-19-92 |
Shut down #6 FES because of oil leak from
pump |
| 4-22-92 |
Row #4 slicing valve jacked open manually,
hand valve on main side closed |
| 4-28-92 |
Must operate #6 FES manually , no auto
controls |
| 5-06-92 |
#2 vilter kicked out breaker and low oil
pressure |
| 5-12-92 |
Lost #5 FES on motor overload |
| 5-15-92 |
#5 FES kicked out, low oil pressure |
| 5-22-92 |
#3 Blast removed 10 amp fuse and installed
25 amp fuse to make fan run |
| Date By Which Violation Must be Abated: |
03/01/98 |
| Proposed Penalty: |
$7000.00 |
Citation 1 Item 9b Type of Violation: Serious
29 CFR 1910.119(e)(3)(iii): The process hazard analysis did not address
the engineering and administrative controls applicable to the hazards and their
interrelationship, such as, appropriate of detection methodologies to provide early
warning of releases:
- At the facility the process hazard
analysis (PHA) for the ammonia
refrigeration unit, including the engine room did not address application of detection
methodologies for ammonia nor did it address requirements for emergency ventilation in the
absence of class 1, division II classification.
- At the facility, the PHA for the ammonia refrigeration unit, did
not address the pressure relief valves and their vent header.
- At the facility, the PHA for the ammonia refrigeration unit, did
not address the emergency isolation valves such as the King Valves, emergency compressor
shutoff switches including their location and access.
- At the facility, the PHA for ammonia refrigeration unit, did not
address the mechanical integrity procedures for equipment including but not limited to
pressure vessels, piping, and shutoff valves, and interlocks to determine their
effectiveness, the integrity of the equipment, the adequacy of the Armour-flex insulation,
and appropriate inspection frequencies and content.
| Date By Which Violation Must be Abated: |
03/01/98 |
Citation 1 Item 9 c Type of Violation: Serious
29 CFR 1910.119(e)(3)(iv): "The process hazard analysis did not address the
consequences of failure of engineering and administrative controls:
At the facility, the PHA did not address the consequences of failure of engineering and
administrative controls such as the continuously operated mechanical ventilation system,
compressor cutouts, PRVs, ammonia detection system, mechanical integrity program, and
contractor program.
| Date By Which Violation Must be Abated: |
03/01/98 |
Citation 1 Item 9d Type of Violation:
Serious
29 CFR 1910.119(e)(3)(v): The process hazard analysis did not address facility
siting:
- The process hazard analysis did not address facility siting issues such as but not
limited to the location of PRV discharge, ignition sources, location of machine room and
control rooms, sufficiency of access or egress for maintenance or emergencies, location of
nearby equipment, and drainage or diking for containing ammonia spills in the machine room
or on the roof.
| Date By Which Violation Must be Abated: |
03/01/98 |
Citation 1 Item 9e Type of Violation: Serious
29 CFR 1910.119(e)(3)(vi): The process hazard analysis did not address human factors:
The process hazard analysis did not address human factors issues including but not limited
to operator/process interface, workplace/working environment, organization/policies, task
design/job organization, training/education, unusual work schedules, location of isolation
valves, clarity and simplicity of displays, clarity of signs and codes, and written
procedures.
| Date By Which Violation Must be Abated: |
03/01/98 |
Citation 1 Item 10 Type of Violation:
Serious
29 CFR 1910.119(e)(5): The employer did not establish a system to promptly address the
process hazard analysis team's findings and recommendations and to communicate the actions
to be taken, as a result of the process hazard analysis team's recommendations, to
operating, maintenance and other employees whose work assignments are in the process and
who could be affected by the recommendations actions:
- At the facility, the recommendations resulting from the 1994 process hazard
analysis (PHA) for the ammonia refrigeration plant were not resolved in a timely manner in
that, on or about April 9, 1997 the following recommendations, were still not completed.
A remote switch was not installed.
Instruction to contractors working on compressors not followed or enforced.
SOP's are not reviewed since they have not been completed.
Plant wide inspection of pipe hangers has not been completed.
Piping that has had an ammonia leak is not properly evaluated and corrections made.
- Recommendations from PHAs were not discussed with operators.
| Date By Which Violation Must be Abated: |
04/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 11 Type of Violation:
Serious
29 CFR 1910.119(f)(1): The employer did not develop and implement written operating
procedures that provided clear instructions for safety conducting activities in each
covered process consistent with the process safety information and which addressed the
elements listed in 29 CFR 1910.119(f)(1)(i) through (f)(1)(v):
At the facility, the written operating procedures for the old unit were
in the process of being rewritten but had only been completed for the compressors.
Operating procedures for operations involving receivers, accumulators, condensers, and
evaporators had not been completed. Presently three sets of procedures are available, each
in different format and level of detail.
| Date By Which Violation Must be Abated: |
06/26/98 |
| Proposed Penalty: |
$7000.00 |
Citation I Item 12a Type of Violation:
Serious
29 CFR 1910.119(f)(1)(i)(B): The employer's written operating procedures covering the
steps for each operating phase did not address normal operations:
At the facility, the written operating procedures for the old and new
ammonia refrigeration units did not have normal operating procedures including data to be
collected during normal walk around such as liquid levels in surge drums and receivers,
inspections on equipment and tasks to be performed such as defrosting evaporators,
instrument readings data to be collected, operating conditions (e.g., temperature,
pressure, flow, etc.), when to perform ammonia transfer operations, and responding to
routine alarms and hammering or other unusual noises.
| Date By Which Violation Must be Abated: |
06/28/98 |
| Proposed Penalty: |
$7000.00 |
Citation 1 Item 12b Type of Violation: Serious
29 CFR 1910.119(f)(1)(i)(C): The employer's written operating procedures covering the
steps for each operating phase did not address temporary operations:
OR IN THE ALTERNATIVE
29 CFR 1910.119(f)(1)(i)(E): The employer's written operating procedures covering the
steps for each operating phase did not address emergency operations:
At the facility, for both the old and new units, there were not temporary or emergency
operating procedures listed for system upsets including operating outside normal operating
limits, operating without safety systems, online maintenance of instruments, interlocks,
and alarms, partial loss of utilities or loss of backup power, extreme weather not
requiring shutdown, operation when the computer system goes down or locks up in an unknown
condition.
| Date By Which Violation Must be Abated: |
06/28/98 |
Citation 1 Item 12cType of Violation: Serious
29 CFR 1910.119(f)(1)(i)(D): The employer's written operating procedures covering the
steps for each operating phase did not address emergency shutdown including the conditions
under which emergency shutdown is required, and the assignment of shutdown responsibility
to qualified operators to ensure that emergency shutdown in a safe and timely manner:
- At the facility, the written operating procedures did not have adequate emergency
shutdown procedures for abnormal or emergency conditions in that they did not define all
conditions in which shut down is required and evacuation is necessary, such as failure of
components (pipes, compressors, vessels) to contain ammonia, fire, critical safety system
failure such as compressor cutouts, or exceeding safe operating limits.
- The operating procedures did not explain how to determine when it is safe to enter
the engine room or what personal protective equipment to wear before entering to isolate
and purge leaking equipment.
| Date By Which Violation Must be Abated: |
06/28/98 |
Citation 1 Item 13
Type of Violation:
Serious
29 CFR 1910.119(f)(1)(ii): The employer's written operating procedures did not address the
requirements for the operating limits listed in 29 CFR 191.119(f)(1)(ii)(A) and (B):
At the facility, the following written operating procedures did not address operating
limits such as flow rates, pressure limits, temperature ranges, and levels operating
procedures also consequences of deviating from operating limits, and steps required to
correct or avoid deviations from those limits, and the consequences of those deviations
for startup, normal, and shutdown operations.
FRICK/IMECO AMMONIA EVAPORATIVE CONDENSERS
FRICK/IMECO AMMONIA EVAPORATORS
FRICK/IMECO AMMONIA COMPRESSORS
HANSEN AND YORK AMMONIA PUMPS
FRICK LOW PRESSURE ACCUMULATOR
FRICK THERMOSYPHON RECEIVER
KLEEN-AIR AMMONIA MAKE-UP AIR UNIT RMAU-1
FRICK SCREW COMPRESSORS
HANSEN AMMONIA PURGER
FES SCREW COMPRESSORS
SOP's #101-121
| Date By Which Violation Must be Abated: |
06/28/98 |
| Proposed Penalty: |
$7000.00 |
Citation 1 Item 14 Type of Violation:
Serious
29 CFR 1910.119(f)(1)(iii)(A): The employer's written operating procedures covering safety
and health considerations did not address the properties of, and hazards presented by the
chemicals used in the process:
At the facility, the following written operating procedures and safe work practices such
as line breaking did not address the hazards such as thermal expansion of trapped liquids,
sudden deceleration of liquid line flow, liquid propelled by high velocity vapor, water
contamination, liquid spills while cleaning suction strainers and demisters, and draining
oil pots.
| Date By Which Violation Must be Abated: |
06/28/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 15 Type of Violation:
Serious
29 CFR 1910.119(f)(1)(iv): The employer's written operating procedures did not address
requirements for the safety systems and their functions:
At the facility, the written operating procedures did not address the function of safety
systems such as: emergency stop buttons, isolation devices (King Valves), level cutouts,
water spray systems, and emergency backup power.
| Date By Which Violation Must be Abated: |
06/28/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 16 Type of Violation: Serious
29 CFR 1910.119(f)(3): The employer did not certify annually that the operating
procedures are current and accurate:
At the facility, the employer did not conduct an annual review of the written operating
procedures and certify that they were current and accurate.
| Date By Which Violation Must be Abated: |
06/28/98 |
| Proposed Penalty: |
$2250.00 |
Citation 1 Item 17 Type of Violation: Serious
29 CFR 1910.119(f)(4): The employer did not develop and implement safe work practices
for employees and contractor employees to provide for the control of hazards during
operations such as lockout/tagout; confined space entry; opening process equipment or
piping; and control over entrance into a facility by maintenance, contractor, laboratory,
or other support personnel:
-
At the facility, the employer failed to implement safe work practices for the
control over entrance into the facility by contractors maintenance personnel working on
the ammonia refrigeration units including providing operator escorts, assuring equipment
is prepared for work, and assuring contractor employee(s) are following safety and health
rules.
- At the facility, the employer failed to develop and implement safe work practices
for opening process equipment or piping. The employer had developed a line break permit,
but no procedure was available which assigned responsibility for approvals, evacuation,
and purging requirements, auditing for compliance, training, and personnel protection
equipment requirements.
| Date By Which Violation Must be Abated: |
06/28/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 18 Type of Violation: Serious
29 CFR 1910.119(g)(2): The employer did not provide refresher training at least every
three years, and more often if necessary, to each employee involved in operating a process
and did not consult with employees in determining the appropriate frequency interval for
refresher training:
- At the facility, the employer did not provide refresher training at least every
three years, and more often if necessary, for employee(s) operating the old refrigeration
unit.
- At the facility, the employer did not consult with employee(s) concerning the
frequency of their need for refresher training.
| Date By Which Violation Must be Abated: |
06/28/98 |
| Proposed Penalty: |
$2250.00 |
Citation 1 Item 19 Type of Violation: Serious
29 CFR 1910.119(g)(3): The employer did not prepare a record which contained the
identity of the employee and the date that training was completed and did not verify that
the employee had received and understood the training required by 29 CFR 1910.119(g):
- At the facility, there was no documentation of training on specific in-plant
operating procedures, operating limits, safety systems, emergency procedures, and safe
work practices and no documentation of the mean that the employer used to verify that the
employees' understood the training that they received including startup, shutdown, and
operation of the new computerized system.
- The employer did not ascertain that each employee involved in operating the
refrigeration unit received and understood the training in that the employer had not
specified knowledge requirements for qualified operators including job skills
demonstration on in-plant equipment and SOP's.
| Date By Which Violation Must be Abated: |
06/28/98 |
| Proposed Penalty: |
$2250.00 |
Citation 1 Item 20 Type of Violation:
Serious
29 CFR 1910.119(h)(2)(i): The employer, when selecting a contractor, did not obtain and
evaluate information regarding the contract employer's safety performance and programs:
- At the facility, the employer did not obtain and evaluate information regarding the
following contract employers' safety performance and programs:
American Systems, Inc.
Dual-Temp Illinois, Inc.
Wachter Electric
Preston Refrigeration
| Date By Which Violation Must be Abated: |
01/01/98 |
| Proposed Penalty: |
$2250.00 |
Citation 1 Item 21 Type of Violation: Serious
29 CFR 1910.119(h)(2)(v): The employer did not periodically evaluate the performance of
contract employers in fulfilling their obligations as specified in 29 CFR 191.119(h)(3):
- At the facility, the employer did not develop and implement a program to
periodically evaluate the performance of contract employers in fulfilling their
obligations as specified in 29 CFR 1910.119(h)(3) in that, the Armour Swift-Eckrich
Contractor Safety Program did not indicate: (1) who could perform the audits and what
their training or experience requirements were; (2) what guidelines would be used to
qualify contractors and how they would be graded prior to awarding contracts; (3) require
all deficiencies found in the contractor safety evaluation and periodic audits have a full
explanation, that findings and any corrective actions be reviewed with the contractor,
that follow-up be performed to ensure corrective actions are completed, and that results
are documented; and (4) what actions would be taken with contractors who had high injury
rates and how resolution would be documented.
- At the facility, the employer did not develop and implement procedures to
periodically evaluate whether contract employee(s) had been trained in safe work
practices, know potential fire, explosion, or toxic release hazards, and applicable
provisions of the emergency action plan. The employer did not develop and implement
procedures to ensure that training and the means to verify contract employees understood
training were documented, and that the training for contractor employees maintaining the
on-going integrity of process equipment was equivalent to that required for direct hire
employees.
| Date By Which Violation Must be Abated: |
01/01/98 |
| Proposed Penalty: |
$2250.00 |
Citation 1 Item 22 Type of Violation:
Serious
29 CFR 1910.119(i)(2)(i): The pre-startup safety review did not confirm
that prior to the introduction of highly hazardous chemicals to the process, construction,
and equipment was in accordance with design specifications:
- At the facility, the pre-startup safety review did not confirm that
prior to the introduction of highly hazardous chemicals to a process, construction, and
equipment was in accordance with design specifications in that process safety information
such as P&ID's wee not compiled and verified as complete, current, and accurate.
- At the facility, the pre-startup safety review did not confirm that
prior to the introduction of highly hazardous chemicals to a process, construction, and
equipment was in accordance with design specifications in that a pre-startup acceptance
test was not performed which included: testing of computer hardware and software;
functional testing of protection devices including alarms, interlocks, cutouts, and level
controls.
| Date By Which Violation Must be Abated: |
02/01/98 |
| Proposed Penalty: |
$70000.00 |
Citation 1 Item 23 Type of Violation: Serious
29 CFR 1910.119(i)(2)(ii): The pre-startup safety review did not confirm that prior to
the introduction of highly hazardous chemicals to the process, the safety, operating,
maintenance, and emergency procedures were in place and were adequate:
At the facility, the operating procedures for the initial startup of the new unit were
inadequate in that they did not explain the initial startup sequence for the complete unit
including: cleaning equipment; closing all drain valves; evacuation, dehydration, leak
checking; charging ammonia; the interrelationships between startup of equipment such as
but not limited to liquid ammonia pumps and main screw compressors; safety interlock
bypasses during startup, operating the computer system, and switching from manual to
computer operation.
| Date By Which Violation Must be Abated: |
02/01/98 |
| Proposed Penalty: |
$7000.00 |
Citation 1 Item 24 Type of Violation: Serious
29 CFR 1910.119(i)(2)(iii): The pre-startup safety review did not confirm that prior to
the introduction of highly hazardous chemicals to a process, for new facilities, a process
hazards analysis a process hazards analysis had been performed and recommendations
had been resolved or implemented before startup; and modified facilities meet the
requirements contained in management of change, paragraph (1):
The employer did not perform a process hazards analysis of the new ammonia
refrigeration unit prior to startup in July 1996 which met the requirements of 29 CFR
1910.119(e)(1) through (e)(7) including an evaluation of safety systems and interlocks,
failure modes of safety systems and the computer system, adequacy of written operating
procedures.
| Date By Which Violation Must be Abated: |
02/01/98 |
| Proposed Penalty: |
$7000.00 |
Citation 1 Item 25 Type of Violation: Serious
29 CFR 1910.119(i)(2)(iv): The pre-startup safety review did not confirm that prior to
the introduction of highly hazardous chemicals to the process, training of each employee
involved in operating a process had been completed.
For the new unit, the employer did not train employees in operating procedures
including initial startup, operating, safety, emergency, and maintenance procedures and
document the training and means to verify that employees understood the training prior to
start up.
| Date By Which Violation Must be Abated: |
02/01/98 |
| Proposed Penalty: |
$7000.00 |
Citation I Item 26 Type of Violation: Serious
29 CFR 1910.1190)(2): The employer did not establish and implement written procedures to
maintain the on-going mechanical integrity of process equipment:
- At the facility, the employer had not developed written procedures for the repair of
process equipment to maintain the ongoing integrity of equipment including the following
pressure vessels and storage tanks, piping, valves, controls, pumps, and compressors.
These procedures shall include materials and spare parts control, authorizations and
approval for repairs, steps to accomplish for repairing or replacing equipment, frequency
of replacement employee training and qualifications, welding and heat treating
requirements, inspection and testing after repair, and documentation requirements.
Pressure Vessels and Storage Tanks Repair, Rerating and Replacement
35# Accumulator
75# Receiver
Transfer Tank
Surge Drums
Heat Exchangers
Piping Repair, Rerating and Replacement
Hot Gas Return Lines
High Temperature Liquid Lines
Hot Gas Lines
Relief Valve Headers
Instruments and Controls Calibration, Repair and Replacement
Level Indicators
Compressor Cutouts
Level Cutouts
Relief Devices Replacement
Refrigeration Valves Repair and Replacement
King Valves
Pump Out Valves
Check Valves
Float Valves
Solenoid Valves
Pump and Compressor Repair and Replacement
Ammonia Pumps
FES #1 through #8 Compressors
- At the facility, the employer had not developed and implemented written procedures
for the replacement or pressure relief valves as evidenced by the fact that the pressure
relief valves for the following equipment had never been replaced:
Innercooler
75# Receiver
35# Receiver
#1 Lowside Dump
#2 Lowside Dump
#3 Lowside Dump
Ice Maker
Transfer Tank
| Date By Which Violation Must be Abated: |
06/26/98 |
| Proposed Penalty: |
$7000.00 |
Citation 1 Item 27 Type of Violation:
Serious
29 CFR 1910.1190)(4)(i): Inspections and tests were not performed on process equipment:
a. At the facility, independent five year inspections and tests were not performed on the
following vessels:
Pilot Receiver
Pump Out Accumulator
25# Accumulator
3# Accumulator
Intercooler
35# Receiver
75# Receiver
#1 Dump Trap/3# Low Side
#2 Dump Trap/3# Low Side
#3 Dump Trap/3# Low Side
#1 Dump Trap/25# High Side
#2 Dump Trap/25# High Side
#3 Dump Trap/25# High Side
Transfer Tank
b. At the facility, inspection and testing was not performed for the following section
of piping and components:
Hot Gas Return Lines
High Temperature Liquid Ammonia Lines
Hot Gas Lines
Relief Valve Headers
Valves on hot gas line, hot gas return line, high temperature liquid lines, and suction
line to #2 cooler
c. At the facility, inspection and testing was not performed for the following
pressure relief valves:
#1 FES COMP
#4 FES COMP
#7 FES COMP
#2 high side dump
75# receiver
oil accumulator
transfer tank |
#2 FES COMP
#5 FES COMP
#8 FES COMP
#3 high side dump
35# receiver
#1 lowside dump
oilpots |
#3 FES COMP
#6 FES COMP
#1 high side dump
innercooler
pumpout accumulator
#2 lowside dump
ice maker |
d. At the facility, inspection and testing was not performed for emergency shutdown
systems including but not limited to:
Compressor cutouts including discharge temperature, discharge pressure, oil temperature
(upper and lower), oil sump temperature maximum.
King Valves
Frick Low Pressure Accumulator high and low liquid level cutouts
25# intercooler high liquid level cutout
e. At the facility, inspection and testing was not performed for controls (including
monitoring devices and sensors, alarms, and interlocks) such as, but not limited to, the
following:
Ammonia detection system
Compressor liquid level control sensors
Compressor thermostats
Compressor liquid level controls
Pump out system level alarms
25# intercooler liquid level alarms
25# intercooler liquid level control
f. At the facility, inspection and testing was not performed for pumps and
compressors, including but not limited to:
FES #1 through #8 Screw Compressors
| Date By Which Violation Must be Abated: |
06/26/98 |
| Proposed Penalty: |
$7000.00 |
Citation 1 Item 28 Type of Violation: Serious
29 CFR 1910.1190)(4)(ii): The employer did not establish and implement written testing
and inspection procedures that followed recognized and generally accepted good engineering
practices:
- At the facility, the Mechanical integrity Program, as implemented, did not follow
good engineering practice. Good engineering practices for testing and inspection programs
include:
The identification and characterization of equipment
The establishment and implementation of testing and inspection procedures for process
equipment that describe the rationale for performing inspections, calibration of
equipment, and the methodology for performing the inspection.
The definition of appropriate frequencies for testing and inspection of process
equipment.
The qualification and training requirements for inspecting and testing personnel.
Criteria for acceptable test results
The establishment of methods to analyze inspection and testing results to assure that
equipment deficiencies are corrected when outside acceptable limits.
- At the facility, the Mechanical Integrity Program did not include procedures for
the inspection and testing of vessels and heat exchangers that followed good engineering
practice. Good engineering practices for the inspection and testing of vessels and heat
exchangers include:
Annual external visual inspections of the condition of insulation and
inspection of nozzles, sight glasses, supports and associated equipment for vibration and
corrosion.
Additional testing and inspection including inspection of the
underlying vessel or heat exchanger when insulation is unsound or damaged.
The need of an independent full inspection every five years including
evaluation of the potential for stress corrosion cracking.
When non-destructive testing such as hydraulic or ultrasonic tests are
necessary, including when sections of insulation on vessels and heat exchangers which are
obviously in poor condition and the insulation must be removed to determine the integrity
of the vessels or heat exchangers.
- At the facility, the Mechanical Integrity Program did not include
procedures for the inspection and testing of piping and components that followed good
engineering practice. Good engineering practices for the testing and inspection of piping
and components include:
The establishment and implementation of testing and inspection
procedures and frequencies that describe the external inspections of piping, valves, and
pressure relief valve headers including, but not limited to inspection for leaks in the
process lines, proper bolting at flanges, inspection for misalignment and vibration,
inspection of supports for hanger distortion or breakage, loose brackets, support
corrosion, shoes off support, corrosion, and damaged insulation.
When non-destructive testing such as hydraulic or ultrasonic tests are
necessary, including when sections of insulation on piping which are obviously in poor
condition and the insulation must be removed to determine the integrity of the piping.
- At the facility, the Mechanical Integrity Program did not include
procedures for the inspection and testing of pressure relief valves and vent systems that
followed good engineering practices. Good engineering practices for the testing and
inspection of pressure relief valves and vent systems include:
Testing and inspection procedures and frequencies and describe visual
onstream inspections and inspection of valves upon removal from service.
The external/onstream inspection of relief devices shall include, but
is not limited to ensuring the correct relief device is installed, the established test or
replacement interval is not exceeded; there are no gags, blinds, closed valves or piping
obstructions; the relief device does not leak; upstream and downstream block valves are
sealed or chained and locked in the proper position; vent stacks and discharge piping are
properly supported; valve body drains and vent stack drains are open; and inspection for
vibration damage.
The employer did not develop and implement inspection and testing
procedures that verified replacement every five years is an adequate interval. To assure
pressure relief valves are still operational when replaced, they must be visually
inspected for corrosion of fouling when removed from service, pop tested in the "as
received" condition by an authorized testing laboratory, and the testing and
inspection or replacement interval reduced, if necessary.
- At the facility, the Mechanical Integrity Program did not include
procedures for the inspection and testing of emergency shutdown systems that followed good
engineering practices. Good engineering practices for the testing and inspection of
emergency. shutdown systems include:
The identification and characterization of equipment including but not
limited to, compressor cutouts, level cutouts, and King valves.
The establishment and implementation of testing and inspection
procedures and frequencies, proper functioning complete instrument loops for cutouts, King
valves, and safety interlocks.
- At the facility, the Mechanical Integrity Program did not include
procedures for the inspection and testing of controls (including monitoring devices and
sensors, alarms, and interlocks) that followed good engineering practices. Good
engineering practices for the testing and inspection of controls (including monitoring
devices and sensors, alarms, and interlocks) include:
The identification and characterization of equipment including flow,
level, temperature, and pressure instruments; automatic controls and control valves,
transmission systems for measurement and control, electrical power systems for
instruments, instrument panels, analyzers and sampling systems.
The establishment and implementation of testing and inspection
procedures and frequencies; functional testing of protection device including alarms,
interlocks, and control valves; calibration of pressure, temperature, and level gauges;
proper support of valves and solenoids; corrosion of equipment and wiring or mechanical
deterioration of equipment; and testing and calibration that is required.
- At the facility, the Mechanical Integrity Program did not include
procedures for the inspection and testing of pumps, compressors, and their drivers that
followed good engineering practices. Good engineering practices for the testing and
inspection of pumps, compressors, and their drivers include:
The identification and characterization of equipment
The establishment and implementation of testing and inspection
procedures and frequencies including but not limited to: (1) external inspections of pumps
and compressors for external visible defects such as unusual noise and vibration, leaks,
misalignment; belts or coupling tension; lubricating oil temperatures and cooling water
temperatures and pressure; pressure gauges and flow meters for proper performance;
cavitation, piping stresses, foundation deterioration, improper operation (excess speed,
lack of lubricant, excess temperature or pressure); and (2) internal inspections for
erosion, corrosion, cracking, etc.
| Date By Which Violation Must be Abated: |
06/26/98 |
| Proposed Penalty: |
$7000.00 |
Citation 1 Item 29 Type of Violation:
Serious
29 CFR 1910.1190)(4)(iv): The employer did not document each inspection and test that
had been performed on process equipment including the date of the inspection or test, the
name of the person who performed the inspection or test, the serial number or other
identifier of the equipment on which the inspection or test was performed, a description
of the inspection or test performed, and the results of the inspection or test:
- At the facility, the employer did not document the name of the inspector who
performed the test or inspection on the following process equipment:
Evaporators UC 1 thru UC 11, UC 12 thru UC35, UC38 thru UC39, UC40 thru UC45, UC48 thru
UC69, UC79 thru UC82, UC89 thru UC91, 387378-2, 387379-2, 387381-2, 387380-2, 2560-82D.
- At the facility, the employer did not document the name of the
inspector who performed the test or inspection nor the date it was performed on the
following process vessels:
Pilot Receiver
Pump Out Accumulator
25# Accumulator
3# Accumulator
Intercooler
35# Receiver
75# Receiver
#1 Dump Trap/3# Low Side
#2 Dump Trap/3# Low Side
#3 Dump Trap/3# Low Side
#1 Dump/25# High Side
#2 Dump/25# High Side
#3 Dump/25# High Side
| Date By Which Violation Must be Abated: |
06/26/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 30 Type of Violation:
Serious
29 CFR 1910.1190)(5): The employer did not correct deficiencies in equipment in a safe and
timely manner:
At the facility, the employer did not correct deficiencies in the following equipment
in a safe and timely manner:
Armour-flex insulation on piping was not replaced when it was known for sixteen years that
it was inadequate in high moisture operations.
Sections of pipe were corroded away up to 90% of original thickness.
Pump out valve stems had corroded to one third the original size and handles were breaking
when employee(s) tried to use them.
Failure to repair/replace the inoperable ammonia sensor/alarm located on the control panel
in the old engine room.
Pressure gauges on the Ammonia T-2 H.T. Pump Receiver vessel were not operational.
In the manufacturing room- hand valves were not readily accessible due to being covered
with insulation.
| Date By Which Violation Must be Abated: |
06/26/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 31
Type of Violation: Serious
29 CFR 1910.1190)(6)(ii): In the construction of new plants and
equipment, the employer did not performed appropriate checks and inspections to assure
that equipment was installed properly and consistent with design specifications and the
manufacturer's instructions:
At the facility, the employer did not develop and implement written
procedures to assure that appropriate checks and inspections were performed and documented
for equipment in the new refrigeration plant to assure that the installation was
consistent with design specifications and the manufacturer's instructions. Appropriate
checks and inspections include:
Evaluation of the construction contractor Quality Control Plan
Review/Approval of drawings "For Construction"
Incoming material inspection
Verification of appropriately qualified craftsmen including welder qualifications and
procedures
Pressure testing
Resolution of nonconformities
Identification of baseline inspection data such as thickness readings
Receipt of equipment data sheets and documentation of tests and inspections
| Date By Which Violation Must be Abated: |
06/26/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 32 Type of
Violation: Serious
29 CFR 1910.1190)(6)(iii): The employer did not assure that maintenance
materials, spare parts and equipment were suitable for the process application for which
they were used:
At the facility, the employer did not assure that the following
maintenance materials, spare parts and equipment were suitable for the process application
or which they were used:
The replacement pressure relief devices for several of the Frick
compressors in the old machine room were not suitable in that they leaked to the engine
room workplace atmosphere when the relief device activated.
| Date By Which Violation Must be Abated: |
01/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 33 Type of Violation: Serious
29 CFR 1910.1190)(1): The employer did not establish and implement
written procedures to manage changes to process chemicals, technology, equipment, and
procedures; and, changes to facilities that affect a covered process:
- At the facility, the employer did not establish and implement written
procedures to include the following:
A definition of roles and responsibilities of key personnel including
senior management, management of change reviewers, and levels of authorization required.
Documentation requirements including the technical basis of the change
(i.e., reasons for performing the work, desired results, technical design, and appropriate
implementation instructions), the type of safety and health hazards evaluation to perform,
requirements to update P&ID's and SOP's.
A definition of the scope of the management of change system to include
personnel changes, organizational changes, and titles and roles of key personnel on all
shifts.
Did not specify training requirements for personnel initiating and
implementing changes and methods of communicating changes to operators, maintenance
technicians, engineers and managers prior to operating the unit.
Did not specify guidelines for special situations such as bypasses of
safety or electrical equipment, operating outside of safe operating limits.
- A management of change was not performed for the following changes,
on or about April 28, 1997:
- The ammonia alarm sensor in the new engine room was disabled on May
25, 1997 and August 22, 1997.
- The 25# intercooler liquid level alarm set point was altered on or
about June 12, 1997.
- Use of #3 and #4 blast for storage of ammonia on or about June 14,
1997.
- Change in type of insulation being installed on ammonia piping and
valves since February 1997.
- Changes to the make-up air intakes in the new engine room along the
west wall.
- Relocation of the relief vent manifold pipe on the new engine roof
away from exit way.
- Changes in facilities including evacuation routes.
| Date By Which Violation Must be Abated: |
02/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 34a Type of Violation: Serious
29 CFR 1910.1190)(2)(i): The written procedures to manage changes did not
assure that the technical basis for the proposed change were addressed prior to any
change:
At the facility, the company did not adequately address the technical basis for the
proposed changes such as but not necessarily limited to, the reasons for performing the
work, desired results, technical design, and appropriate implementation instructions, for
the following changes:
- The Blast Freezer relay logic control replacement with a Programmable
Logic Control on or about April 14, 1996.
- The addition of valves during the replacement of a transfer tank in the engine room on
or about October 4, 1996.
- The addition of valves in the pump-out line for row #6 on or about November 2, 1996.
- For the addition of 2 six inch isolation valves in the compressor discharge mainline on
or about May 24, 1997.
| Date By Which Violation Must be Abated: |
02/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 34b Type of Violation: Serious
29 CFR 1910.1190)(2)(ii): The procedures to manage changes did not
assure that the impact on safety and health for the proposed change was addressed prior to
any change:
At the facility, the company did not adequately address the impact on
safety and health for the proposed changes, in that the Safety Review Checklists were not
completed in full detail, such as but not necessarily limited to:
- For the Blast Freezer relay logic control replacement with a
Programmable Logic Control on or about April 14, 1996, a PHA was not performed and the
"Safety Review Checklist" and "Pre-Startup Safety Review
Verifications" were not completed.
- The addition of valves during the replacement of a transfer tank in
the engine room on or about October 4, 1996, the Pre-Startup Safety Review Verification
sheet was blank.
- The addition of valves in the pump-out line for row 36 on or about
November 2, 1996 did not address impact on safety and health in that the Pre-Startup
Safety Review Verification was not completed, and LO/TO was not performed.
- The May 24, 1997 replacement of ammonia mains" and installation
of two 6 inch valves did not address the impact on safety and health of changes in
procedures while burning off air/ammo gas after evacuating ammo header.
| Date By Which Violation Must be Abated: |
02/01/98 |
Citation 1 Item 34c Type of Violation: Serious
29 CFR 1910.1190)(2)(iii): The procedures to manage changes did not assure
that modifications to operating procedures or proposed change was addressed prior to any
change:
At the facility, the company did not adequately address the modifications to operating
procedures for the proposed changes, such as but not necessarily limited to:
- Addition of the new FES screw compressor #8 and IMECO condenser on or
about October 21, 1994.
- The Blast Freezer relay logic control replacement with a Programmable Logic Control on
or about April 14, 1996.
- The addition of valves during the replacement of a transfer tank in the engine room on
or about October 4, 1996.
- The addition of valves in the pump-out line for row #6 on or about November 2, 1996.
- For the addition of two 6 inch isolation valves in the compressor discharge main line
on or about May 24, 1997.
| Date By Which Violation Must be Abated: |
02/01/98 |
Citation 1 Item 35 Type of Violation: Serious
29 CFR 1910.119(l)(4): When a change covered by this paragraph resulted in
a change in the process information, such information was not updated accordingly:
At the facility the process safety information was not updated when changes, such as but
not necessary limited to the following, were made:
- Addition of the new FES screw compressor #8 and IMECO condenser on or
about October 21, 1994.
- The Blast Freezer relay logic control replacement with a Programmable Logic Control on
or about April 14, 1996.
- The addition of valves during the replacement of a transfer tank in the engine room on
or about October 4, 1996.
- The addition of valves in the pump-out line for row #6 on or about November 2, 1996.
- For the addition of two 6 inch isolation valves in the compressor discharge main line
on or about May 24, 1997.
| Date By Which Violation Must be Abated: |
02/01/98 |
| Proposed Penalty: |
$2250.00 |
Citation 1 Item 36 Type of
Violation: Serious
29 CFR 1910.1190)(5): When a change covered by this
paragraph resulted in a change in the operating procedures or practices required by
paragraph (f) of this section, such procedures or practices were not updated accordingly:
At the facility, the company did not implement either
the modifications to existing or additions of new operating procedures or practices for
the changes such as but not necessarily limited to:
- The ammonia alarm sensor in the new engine room was disabled on May
25, 1997 and August 22, 1997.
- The 25# intercooler liquid level alarm set point was altered on or
about June 12, 1997.
- Use of #3 and #4 blast for storage of ammonia on or about June 14,
1997.
- Change in type of insulation being installed on ammonia piping and
valves since February 1997.
- Failure to repair/replace the inoperable ammonia sensor/alarm located
on the control panel in the old engine room.
- Changes to the make-up air intakes in the new engine room along the
west wall.
- Addition of the new FES screw compressor #8 and IMECO condenser on or
about October 21, 1994.
- The Blast Freezer relay logic control replacement with a Programmable
Logic Control on or about April 14, 1996.
- The addition of valves during the replacement of a transfer Link in
the engine room on or about October 4, 1996.
- The addition of valves in the pump-out line for row #6 on or about
November 2, 1996.
- For the addition of two 6 inch isolation valves in the compressor
discharge main line on or about May 24, 1997.
| Date By Which Violation Must be Abated: |
02/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 37 Type of Violation: Serious
29 CFR 1910.119(m)(1): The employer did not investigate each incident which
resulted in, or could reasonably have resulted in, a catastrophic release of a highly
hazardous chemical in the workplace:
- The employer did not develop an incident investigation procedure that spelled out
requirements for investigating each incident which resulted in, or could reasonably have
resulted in a catastrophic release of a highly hazardous chemical in the workplace, and
which describe the following:
Requirements to initiate the incident investigation within 48 hours
following the incident.
Requirements to investigate each incident which resulted in, or could reasonably have
resulted in a catastrophic release of highly hazardous chemical in the workplace
including, but not limited to:
Fatalities
Incidents involving injury to employees
Incidents involving property damage
Fires or explosions and hazardous material releases
Other near-misses such as excursion of process parameters beyond pre-established
"critical" control points, activations of emergency shutdowns, releases of
material that are classified as environmentally reportable events, and activation of
hazards control systems such as safety protective systems (e.g., relief valves, fixed
sprinkler systems).
The makeup of the incident investigation team
The inclusion of contractor employees when they are involved in the incident
The methodology of the incident investigation to thoroughly investigate and analyze the
incident
Training requirements for the team leader and members
Report requirements and retention
The system established to promptly address and resolve incident report findings and
recommendations, and document resolutions and corrective actions taken
The methods used to review incident findings with employees whose job tasks are relevant
to the findings including contract employees where applicable
- At the facility, the following incidents were not investigated:
| 5-02-97 |
Pinhole leaks in #4 condenser |
| 5-05-97 |
Leak in pump out valve |
| 5-09-97 |
Leak in pump line above box room & in-valve for #2
Blast |
| 5-11-97 |
FES #7 sight glass leaking |
| 5-14-97 |
Leak on 25# intercooler |
| 5-18-97 |
Liquid ammonia leak on transfer pump on new system |
| 5-20-97 |
Pump out valves leaking at #1 and #4 FEP |
| 5-25-97 |
NH3 Team venting ammonia vapor outside engine room, vapors
coming back in |
| 5-25-97 |
Leak at pilot receiver sight glass coupling |
| 5-28-98 |
Hot gas leak at NW hot dog pack |
| 6-04-97 |
Pump out valve #2 Blast hi-temp liquid line leaking |
| 6-19-97 |
Leak from low liquid pump |
| 6-21-97 |
Leak on #1 cooler |
| 6-25-97 |
leak on unit #1 Receiving Dock(above scales) |
| 6-27-97 |
Leak at #1 temp cooler, Hot gas valve |
| 7-10-97 |
Leak in #1 cooler |
| 8-12-97 |
Leak at transfer tank float |
| 8-15-97 |
Bad leak at #1 Frick compressor at unloader blocker out
line |
| 8-20-97 |
Contractor turned off the ammonia sensor detection system |
| Date By Which Violation Must be Abated: |
01/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 38 Type of
Violation: Serious
29 CFR 1910.119(m)(3): The incident investigation team did not consist of at least one
person knowledgeable in the process involved, including a contract employee if the
incident involved work of the contractor, and other persons with appropriate knowledge and
experience to thoroughly investigate and analyze the incident:
- At the facility, the employer did not have personnel with training or experience to
thoroughly investigate and analyze the following incidents to determine appropriate
recommendations to prevent the incidents from reoccurring:
6/19/95 ammonia vapor pipe leak due to corrosion in the engine room did not evaluate
the need to implement a mechanical integrity testing and inspection on other sections of
piping or to remove other piping areas with poor insulation.
9/15/96 liquid ammonia pipe leak due to corrosion did not evaluate the need to
implement a mechanical integrity testing and inspection on other sections of piping or to
remove other areas with corrosion.
2/4/97 evaporator leak due to corrosion did not evaluate the need to implement a
mechanical integrity testing and inspection on other evaporators or replace other
evaporators installed at approximately the same time.
2/13/97 evaporator gauge leak due to corrosion did not evaluate the need to implement a
mechanical integrity testing and inspection on other control valve or replace other
controls valves if corroded badly.
6/27/97 ammonia pipe leak due to corrosion on the slicing floor did not evaluate the
need to implement a mechanical integrity testing and inspection on other sections of
piping or to remove other piping area with poor insulation.
- At the facility, no team member had adequate training, knowledge, or experience to
thoroughly investigate and analyze the incident.
| Date By Which Violation Must be Abated: |
01/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 39 Type of Violation: Serious
29 CFR 1910.119(m)(5): The employer did not establish a system to promptly address and
resolve the incident investigation report findings and recommendations:
At the facility, the following incident investigation item was not resolved on or about
April 9, 1997.
| Incident Date |
Recommendation |
| 9/15/96 |
Recommended piping evaluation |
| Date By Which Violation Must be Abated: |
|
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 40 Type of Violation: Serious
29 CFR 1910.119(o)(1): The employer did not verify that the procedures and practices
developed under the standard were adequate and were being followed:
At the facility, the employer did not verify that the procedures and practices developed
under the standard were adequate and were being followed as evidenced by the following
violations of the PSM standard that were not addressed by the 1995 and 1996 compliance
audits.
PSI was not completed
| Date By Which Violation Must be Abated: |
06/26/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 41 Type of Violation: Serious
29 CFR 1910.119(o)(2): The compliance audit was not conducted by at least one person
knowledgeable in the process:
At the facility, the 1995 and 1996 compliance audits were performed without at least
one person with appropriate knowledge, experience, or training to perform a Process Safety
Management program evaluation including evaluating program requirements and documentation,
performing employee interviews, and evaluating of on-site conditions.
| Date By Which Violation Must be Abated: |
06/26/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 42 Type of Violation: Serious
29 CFR 1910.119(o)(4): The employer did not determine and document an appropriate response
to each of the findings of the compliance audit required by 29 CFR 1910.119(o)(1), and
document that the deficiencies had been corrected:
- The following audit findings were not resolved in a timely manner or adequately
explained on or about 4/9/97:
Audit
Date
|
Ref. #
|
Deficiency
|
|
|
|
| 5/10/96 |
PSI A1 & C1 |
PSI not done before PHA |
| 10/25/95 |
PSI A3 |
No Block Flow Diagram |
| 10/25/96 |
PSI A5,B2,C3 |
For old system, no documentation equipment
complies
with good engineering practices. |
| 5/10/96 |
PHA A5 |
PHA does not address previous incidents. |
| 10/25/95 |
PHA A7,A9,Bl,B2,C5 |
PHA recommendation resolution not documented. |
| 10/25/95 |
SOP A1-A9,B4,C1-C4 |
None of the SOP's deficiencies wee corrected. |
| 10/25/95 |
TRA A5,C2 |
Consult with employees, refresher training. |
| 5/10/96 |
TRA C1 |
No documentation of training. |
| 10/25/95 |
CON A2,A5,C6-C7 |
None of the contractor deficiencies were
corrected. |
| 5/10/96 |
CON A3,A4,A6,A8-Al3, B1-B2,C1-C5 |
None of the contractor
deficiencies were corrected. |
| 5/10/96 |
NU A3 |
No documentation of NU training |
| 12/17/96 |
MI C1,C2,C7,C8 |
Inspection and Test Procedures follow food
engineering practice. |
| 12/17/96 |
MOC Al
MOC A9 |
Review of MOC written procedures
SOP's not valid |
| 5/10/95 |
MOC A8 |
PSI not updated |
| 5/10/96 |
IN IV A5
IN IV A6 |
No system to resolve findings
No documentation of resolution |
| 10/25/95 |
EAP C2 |
No first responder training |
| 5/10/96 |
EAP A5
EAP A7
EAP B4 |
Review to determine if it covers small
releases.
Determine if it meets requirements of 1910.120.
Review exit lights |
| Date By Which Violation Must be Abated: |
06/26/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 43 Type of Violation: Serious
29 CFR 1910.120(q)(2): The employer did not develop an emergency response plan for
emergencies which adequately addressed emergency recognition and safe distances and places
or refuge:
- For ammonia releases, the facility's Hazmat Emergency Response procedures contains
inadequate emergency recognition procedures in that it specifies that three conditions be
simultaneously met before any release of ammonia is considered a Hazmat response.
Utilizing the criteria that the release of ammonia needs to exceed the EPA's reportable
quantity is not protective of employee health and safety.
- For Carbon Dioxide or Sulfuric Acid releases, the facility's Hazmat Emergency Response
procedure contains no emergency recognition procedures or protocol.
- For all chemical releases, the facility's Hazmat Emergency Response and Emergency
Action Plan procedures contain inadequate detail and methods to determine and define safe
distances and places of refuge.
| Date By Which Violation Must be Abated: |
12/08/97 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 44 Type of Violation: Serious
29 CFR 1910.132(d)(1): The employer did not assess the workplace to determine if
hazards were present or were likely to he present, which necessitate the use of personal
protective equipment:
At the facility a written workplace hazard assessment was not developed to assess the
hazards presented by potential exposure to liquid or vapor ammonia exposures to operating
engineers during operations such as but not necessary limited to line breaking, valve
replacement, spill response, pipe and equipment leak repair.
| Date By Which Violation Must be Abated: |
12/01/97 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 45 Type of Violation: Serious
29 CFR 1910.134(b)(1): Written standard operating procedures governing the selection
and use of respirators were not developed:
- At the facility, the current written respirator program stated that the only type
of respiratory protection being used were self-contained breathing apparatus, when
canister gas masks were also being used for protection against ammonia.
- At the facility, the current written respiratory program did not address procedures
for the selection and use of respiratory protection when performing emergency response
operations to chemicals present on site including but not necessarily limited to Carbon
Dioxide and Sulfuric Acid.
| Date By Which Violation Must be Abated: |
12/01/97 |
| Proposed Penalty: |
$2250.00 |
Citation 1 Item 46 Type of
Violation: Serious
29 CFR 1910.134(b)(8): Appropriate surveillance of work area conditions and degree of
employee exposure was not maintained:
Ammonia system operators routinely respond to leaks of ammonia from piping, valves and
related refrigeration equipment, by approaching the area of the leak without air sampling
to determine airborne exposure levels. Canister gas masks, or no respiratory protection at
all, are being utilized for protection against unknown concentrations of airborne ammonia,
due to the lack of air monitoring being performed, thereby negating the approval of the
gas mask.
| Date By Which Violation Must be Abated: |
12/01/97 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 47 Type of Violation: Serious
29 CFR 1910.147(c)(3)(i): When a tagout device was used on an energy isolating device,
which was capable of being locked out, the employer did not demonstrate that the tagout
program provided a level of safety equivalent to that obtained by using a lockout program:
In the TRM stuffing department, the Shiramatic machine which has a pneumatic isolation
valve that is capable of being locked-out was observed to be tagged out when the employee
removed the plexiglass guards at the point of operation and reached into the machine to
cut bologna casing material, exposing him to crushing and laceration hazards. The tagout
did not provide equivalent protection in that: 1) The attachment for the tag did not pass
through the locking hole in the isolation valve to provide a physical barrier to closing
the valve and also did not assure that it was in the full off position; 2) Additional
safety measures such as opening or providing of an additional means of isolating the
pneumatic pressure, which could be accomplished by disconnecting the Hansen quick
disconnect in the air line supplying pressure to the Shiramatic machine or by providing an
additional isolation valve, were not utilized.
| Date By Which Violation Must be Abated: |
10/15/97 |
| Proposed Penalty: |
$7000.00 |
Citation 1 Item 48 Type of Violation: Serious
29 CFR 1910.147(c)(4)(ii): The employer did not develop, document and utilize
procedures for potentially hazardous energy which clearly and specifically outline the
scope, purpose, authorization, rules, and techniques to be utilized for the control of
hazardous energy:
Instances include but may not necessarily be limited to the following:
- The procedure for the Shiramatic machine located in the TRM Stuffing Department,
did not address the verification of isolation by the use and reading of the air pressure
gauge on the control panel to assure that air pressure was relieved upon isolation. The
procedure also did not address the procedures to be used by the sanitation crew for
equipment cleanup operations whereby the machine is isolated from the air supply by
disconnection of the Hansen quick disconnect.
- The procedure for the Bolo Cozzini Vacuum Hopper & Mill located in the TRM
Stuffing Department, did not address: 1) isolation of the pneumatic pressure through
closing of the air line valve and placing a lock on it followed by receiving air pressure
in the line by opening the valve located on the bottom of the air dryer/separator and then
verifying relief of air pressure by using the attached air pressure gauge (which was in
inoperable condition), 2) placement of the lid support latches to lock the lid in the open
position.
- Specific step-by-step procedures for lockout/tagout were never developed, which
detailed the rules and techniques to be utilized for the control of hazardous energy, for
the following ammonia refrigeration equipment:
Hansen Auto Purger Non-Condensible Gas Refrigerant Purger
Ammonia Evaporators
Ammonia Sensor
King Valves
General Valve Replacement
Pressure Relief Valve Replacement
Solenoid Valve Replacement
- Specific step-by-step procedures for lockout/tagout did not
adequately detail the rules and techniques to be utilized for the control of hazardous
energy, for the following ammonia refrigeration equipment:
FES #1 through #7 Screw Compressor
Ammonia Transfer System Low Side
3# Accumulator
25# Accumulator
FES #8
25# Ammonia Intercooler
Ammonia Pump Out System
Low Temperature Blast Chillers
North Star Ice Maker
Brine Chiller-KSI Tunnel
Liquid Ammonia Transfer Tank, 35# Receiver to 75# Receiver
Kleen-air Ammonia Make-up Air Unit RMAU-1
Hansen Automatic Purger P-1
Frick Thermosyphon Receiver
Frick/IMECO Ammonia Evaporators EV-2
Hansen Liquid Ammonia Pump AP-1
Hansen Liquid Ammonia Pump AP-2
York Liquid Transfer Pump AP-3
Frick Low Pressure Accumulator
Frick Screw Ammonia Compressor Number RC-2
Frick/IMECO Ammonia Evaporator EC-1 and EC-2
Frick Screw Ammonia Compressor Number RC-1
Frick/IMECO Ammonia Evaporator EV-3 through EV-17
Frick/IMECO Ammonia Evaporator EV-26 through EV-31
Frick/IMECO Ammonia Evaporator EV-5
35# Ammonia Receiver
Pilot Liquid Ammonia Receiver
75# Ammonia Receiver
- Specific procedural steps to cover shift change transfer of lockout or tagout
devices, and the responsibility for them, were not developed for the operators performing
preventive maintenance and repair on ammonia refrigeration equipment.
| Date By Which Violation Must be Abated: |
06/26/98 |
| Proposed Penalty: |
$7000.00 |
Citation 1 Item 49 Type of Violation: Serious
29 CFR 1910.147(c)(6)(i): The employer did not conduct a periodic inspection of the energy
control procedure at least annually to ensure that the procedure and requirements of this
standard are being followed:
At the facility located in Kansas City, Kansas, the energy control program which utilized
both locks and/or tags was not inspected on at least an annual basis to assure that
deviations from the program or inadequacies with the program were identified and
corrected.
| Date By Which Violation Must be Abated: |
01/08/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 50 Type of Violation: Serious
29 CFR 1910.147(c)(7)(i): The employer did not ensure that the purpose and function of the
energy control program was understood and that the knowledge and skills required for the
safe application, usage and removal of energy control devices was acquired by the
employee(s):
At the facility in the manufacturing department employee(s) operating the shiramatic were
exposed to amputations of extremities caused by inadequate lockout/tagout training when
adjusting the clip tightener, clearing staple jamb ups, and other machine adjustments.
| Date By Which Violation Must be Abated: |
10/15/97 |
| Proposed Penalty: |
$7000.00 |
Citation 1 Item 51 Type of Violation: Serious
29 CFR 1910.165(b)(2): The employee alarm system was not capable of being perceived above
ambient noise levels by all employees in the affected portions of the workplace:
The intercom system which is being used to notify employees of the need to evacuate in the
event of a chemical release, was not audible in area such as but not necessarily. limited
to the Cage Wash Area, Acid Wash Area, Browning Room, Cryovac Area, and New Spice Room.
| Date By Which Violation Must be Abated: |
10/04/97 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 52a Type of Violation: Serious
29 CFR 1910.303(f): Each service, feeder and branch circuit, at its disconnecting means or
overcurrent device, was not legibly marked to indicate its purpose, nor located and
arranged so the purpose was evident:
At the facility between 50 - 60 percent of the electrical feed panels had not been
identified, thus exposing employee(s) to electrical hazards while performing any type of
maintenance or preventative maintenance activities.
| Date By Which Violation Must be Abated: |
03/01/98 |
| Proposed Penalty: |
$4500.00 |
Citation 1 Item 52b Type of Violation: Serious
29 CFR 1910.303(g)(2)(i): Live parts of electric equipment operating at 50 volts or more
were not guarded against accidental contact by approved cabinets or other forms of
approved enclosures, or other means listed under this provision:
- Employee(s) working at the reeves drive in the sizzlean area were exposed to
electrical hazards created by the electrical disconnect box being left open exposing the
live conductors.
- Employee(s) working in the old engine room were exposed to electrical hazards created
by the backside access door to the control panel not having a latch to keep it closed.
| Date By Which Violation Must be Abated: |
|
Citation 1 Item 53a Type of Violation: Serious
29 CFR 1910.304(f)(4): The path to ground from circuits, equipment, and enclosures was not
permanent and continuous:
Employee(s) utilizing a fan in the new engine room were exposed to electrical hazards
caused by no ground pin on plug of cord.
| Date By Which Violation Must be Abated: |
|
| Proposed Penalty: |
$2250.00 |
Citation 1 Item 53b Type of Violation: Serious
29 CFR 1910.305(a)(2)(iii)(G): Flexible cords and cables of temporary circuits were not
protected from accidental damage:
Employee(s) working with the shiramatic were exposed to electrical hazards due to the
outer insulation on the cord being broken.
| Date By Which Violation Must be Abated: |
|
Citation 1 Item 53C Type of Violation:
Serious
29 CFR 1910.305(j)(2)(ii): Receptacles installed in wet or damp locations were not
suitable for the location:
A four prong receptacle for the reeves drive in the sizzlean are was not rated for water
tightness when sprayed with water by night time clean-up, thus exposing employee(s) to
electrical hazards.
|
Thomas K. Marple
Area Director |
See pages 1 through 3
of this Citation and Notification of Penalty for information on employer and employee rights and responsibilities.
| Citation and Notification of Penalty |
OSHA-2 (Rev. 6/93) |
U.S. Department of Labor
Occupational Safety and Health Administration
Suite 105
8600 Farley
Overland Park, KS 66212
Phone: (913)236-3220 FAX: (913)236-3224 |
|
INVOICE/
DEBT COLLECTION NOTICE
|
Company Name:
Inspection Site:
Issuance Date: |
Armour Swift - Eckrich, Inc.
4612 Speaker Rd., Kansas City, KS 66110
10/09/97 |
Summary of Penalties for Inspection Number 301340220
Citation 1, Serious
Total Proposed Penalties |
= $ 256650.00
= $ 256650.00 |
To avoid additional charges, please remit payment promptly to this Area Office for the
total amount of the uncontested penalties summarized above. Make your check or money order
payable to: "DOL-OSHA". Please indicate OSHA's Inspection Number
(indicated above) on the remittance.
OSHA does not agree to any restrictions or conditions or endorsements put
on any check or money order for less than full amount due, and will cash the check or
money order as if these restrictions, conditions, or endorsements do not exist.
Pursuant to the Debt Collection Act of 1982 (Public Law 97-365) and
regulations of the U.S. Department of Labor (29 CFR Part 20), the Occupational Safety and
Health Administration is required to assess interest, delinquent charges, and
administrative costs for the collection of delinquent penalty debts for violations of the
Occupational Safety and Health Act.
Interest. Interest charges will be assessed at an
annual rate determined by the Secretary of the Treasury on all penalty debt amounts not
paid within one month (30 calendar days) of the date on which the debt amount becomes due
and payable (penalty due date). The current interest rate is 3 %. Interest will accrue
from the date on which the penalty amounts (as proposed or adjusted) become a final order
of the Occupational Safety and Health Review Commission (that is, 15 working days from
your receipt of the Citation and Notification of Penalty), unless you file a notice of
contest. Interest charges will be waived if the full amount owed is paid within 30
calendar days of the final order.
Delinquent Charges. A debt is considered
delinquent if it has not been paid within one month (30 calendar days) of the penalty due
date or if a satisfactory payment arrangement has not been made. If the debt. remains
delinquent for more than 90 calendar days, a delinquent charge of six percent (6%) per
annum will be assessed accruing from the date that the debt became delinquent.
Administrative Costs. Agencies of the
Department of Labor are required to assess additional charges for the recovery of
delinquent debts. These additional charges are administrative costs incurred by the Agency
in its attempt to collect an unpaid debt. Administrative costs will be assessed for demand
letters sent in an attempt to collect the unpaid debt.
|
|
Thomas K. Marple
Area Director |
Date |
Corrective action, taken by you for each alleged violation should be
submitted to this office on or about the abatement dates indicated on the Citation and
Notification of Penalty.
If the hazards itemized on this citation(s) are not abated/corrected
and a follow-up inspection is conducted, your establishment may receive a Failure to Abate
Citation for the uncorrected hazards with subsequent additional monetary penalties of
up to thirty (30) times the original penalty amount of the uncorrected hazards.
A work sheet has been provided to assist in providing the required
abatement information. A completed copy of this work sheet should be posted at the
worksite with the Citation(s).
| CERTIFICATION OF CORRECTIVE ACTION WORKSHEET |
Company Name:
Inspection Site:
Issuance Date: |
Armour Swift - Eckrich, Inc.
4612 Speaker Rd., Kansas City, KS 66110
10/09/97 |
List the specific method of correction for each item on this citation in this package
that does not read "Corrected During Inspection" and return this page with the
signed Informal Settlement Agreement to: U.S. Department of Labor - Occupational Safety
and Health Administration, Suite 105, 8600 Farley, Overland Park, KS 66212.
|
|
| NAME OF COMPANY OFFICIAL |
DATE |
NOTE: 29 USC 666.(g): Whoever knowingly makes any false statements,
representation or certification in any application, record, plan or other documents filed
or required to be maintained pursuant to the Act shall, upon conviction, be punished by a
fine of not more that $10,000, or by imprisonment for not more than six months or both.
POSTING: A copy of the completed Corrective Action Worksheet should be
posted for employee review.
|
|
|